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						| Project Log:  Thursday, September 9 2010 
 With an unexpected delay at work, I found myself with 
						much of a day available to work on the Fisher.  I 
						continued with some of the parts removal and demolition, 
						beginning with the propeller and shaft.
 
 I removed the propeller with a prop puller with no undue 
						effort.  The brass (or bronze) key in the stainless 
						shaft was well stuck in place, though, and took a while 
						to free so that I could pull the shaft out of the boat 
						through the engine room; the coupling was still 
						attached.
 
 The shaft featured a non-standard taper, and was in only 
						fair condition with some scoring and crevice corrosion, 
						and I'd never anticipated reusing it.  I set it and 
						the propeller aside.
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						| Up in the boat, I removed the remainder of the steering 
						gear, including the heavy cable, brackets, and the 
						entire helm console, which I intended to rebuild along 
						with the remainder of the pilothouse.  With some 
						difficulty I removed the teak wheel, which I hoped to 
						reuse.  I set aside the various pieces of the helm 
						console to use as guidelines for reconstruction later.  
						I also removed a manual bilge pump from the lazarette, 
						plus its related through hull fitting (which unscrewed 
						with only hand pressure).
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						| I removed the "dashboard"--the wide, flat countertop 
						across the front of the pilothouse, which was badly 
						damaged and required replacement; plus it was likely 
						that I'd slightly reconfigure this area, including the 
						companionway.  The dashboard was secured with 
						little nails at the aft end, and glassed to the bulkhead 
						at the forward end; I had to cut the tabbing to remove 
						the shelf.  I knew I'd regret removing this shelf, 
						as it formed a handy place to store tools and such, but 
						I couldn't stand it any longer.
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						| In the cabin, I removed a miscellany of some of the 
						remaining little screwed-in fittings from the bulkheads 
						before it was time to quit for the day.
 
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						| Total Time Today:  4 hours
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